论文部分内容阅读
吐哈油田丘陵采油厂20万方轻烃装置检修后,各项装置运行良好,经过改造的装置运行效果明显,仅原料气压缩机加减载流程和高温干气进原油稳定塔气体两个工艺改造项目年可创造产值980万元。 9月9日至19日,丘陵采油厂对20万方轻烃装置进行了全面检修,检修共涉及12个检修项目和14个工艺改造项目,经过检修后的装置运行良好。其中,原料气压缩机加减载流程改造后,机组开停加减过程中原料气放空减少,火炬黑烟减少,平均每天可节约气0.52万立方米,可产液化气1.3吨,轻油0.35吨,干气0.46万立方米;对高温干气进原油稳定塔气体改造后,保证了原稳气压缩机的正常运转,原油在储运过程中
After the overhaul of 200,000 light hydrocarbon unit in Tuha Oilfield Hilly Oil Production Plant, all the units operated well and the operation effect of the modified unit was obvious. Only the processes of loading and unloading of raw material gas compressor and gas of high temperature dry gas into crude oil stabilized tower were two processes Reconstruction project can create an output value of 9.8 million yuan. From September 9 to 19, the Hilly Oil Production Plant conducted a thorough overhaul of 200,000 light-hydrocarbon units. The overhaul involved a total of 12 overhaul projects and 14 process rebuilding projects. The overhauled units operated well. Among them, the feed gas compressor loading and unloading process transformation, the unit opening and closing process reduce the venting of raw materials to reduce the torch smoke reduction, the average daily gas savings of 5200 cubic meters, can produce liquefied petroleum gas 1.3 tons, light oil 0.35 Ton, dry gas 4600 cubic meters; high temperature dry gas into the gas tower after the transformation of gas to ensure the normal operation of the original gas compressor, crude oil storage and transportation process